During the course of fixing a multitude of problems w/ the 97 GTX I bought last week, I came across an issue w/ the water seperator. When I cleaned it , I didn't like the way it seated. Anyway, after the whole filter / fuel line change, carb cleaning, it would still bog at high end. So I go back to this seperator and it won't tighten anymore w/o jumping a thread, so for the short term, I wipe some Hi-perf Copper Loctite RTV around the seal, let it dry and test drive. NO issues, it runs 7500rpm w/o a hiccup.
If you are having any suspected fuel delivery issues, this can't hurt.
I'm sure someone has submitted a replacement for this OEM part which I'll do during the next cleaning.
Hope it helps someone. Here is a pic.
Steve
If you are having any suspected fuel delivery issues, this can't hurt.
I'm sure someone has submitted a replacement for this OEM part which I'll do during the next cleaning.
Hope it helps someone. Here is a pic.
Steve