LikeabossTM
Active Member
Update, I pulled the carb and checked the ports, all low speed ports are flowing like a fire-hose. As mentioned, the regulator needle lever was about 1mm below the body of the chamber so I bent it back up level. Pop off is now 35-36.
The recently installed carb base gasket looked good, however, I taped some 800 grit sandpaper to a tile and took down the slight squish impressions to flush, and reinstalled it with a little aviation form-a-gasket smeared on that side just in case. Remember that this isn't the thin paper gasket, it's the poly version that's about 3/16" thick so there's lots of material to work with.
Started up in the driveway and pumping wot was crisp while transitioning, so hopefully that's solved the problem I had during the last water test. Crossing my fingers for the next trip to the lake.
The recently installed carb base gasket looked good, however, I taped some 800 grit sandpaper to a tile and took down the slight squish impressions to flush, and reinstalled it with a little aviation form-a-gasket smeared on that side just in case. Remember that this isn't the thin paper gasket, it's the poly version that's about 3/16" thick so there's lots of material to work with.
Started up in the driveway and pumping wot was crisp while transitioning, so hopefully that's solved the problem I had during the last water test. Crossing my fingers for the next trip to the lake.